L-1011 Accidents and Incidents
This is a brief description of the accidents and incidents that
the Lockheed L-1011 has been involved in. There are also some links to
more info that can be found on the internet. Read and learn.
December 29, 1972. |
Everglades, Florida, USA. |
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Eastern Airlines N310EA. |
L-1011-1 (serial no 1011). |
Eastern Airlines flight 401 departed New York for a night flight to Miami. On
approach to Miami the crew did not get a green "down and locked" light for
the nosegear. They aborted the landing and climbed back to 2000 ft. The
Flight Engineer climbed down into the Forward Electronic Service Compartment
(FESC) to visually check the nosegear via a porthole while the rest of the
cockpit crew also tried to solve the problem up in the cockpit. Noone noticed
that the aircraft started a gentle descend which did not stop until the
aircraft crashed. Of the 176 total onboard 99 died.
April 19, 1974. |
Boston, USA. |
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Trans World Airlines (TWA) N31007 |
L-1011-1 (serial no 1026). |
The aircraft was on ground when a fire broke out with major damage to the
rear fuselage as the result. It was never repaired.
August 19, 1980. |
Riyadh, Saudi Arabia. |
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Saudi Arabian Airlines, HZ-AHK. |
L-1011-200 (serial no 1169). |
The flight, originating in Karachi, made an intermediate stop in Riyadh and
then departed for Jeddah. 7 minutes after takeoff, aural and visual warnings
indicated smoke in the aft cargo compartment. The crew initiated a return
to Riyadh from FL220. During the descend smoke was noted in the aft
passenger cabin, the number #2 engine throttle was stuck and passengers
(panicking) were fighting aft of the number 2 doors.
During final approach the #2 engine was shut down and the Captain told
the cabin crew not to evacuate. The aircraft landed at Riyadh runway 01,
taxied to a taxiway and then the crew told the tower that they would shut
down the engines and evacuate. The engines were shut down but no evacuation
was initiated so the fire and rescue personnel tried to open the doors.
After 23 minutes (aircraft still pressurized) they managed to open R2 door.
All 301 onboard were killed, the cause of the fire was never established.
December 23, 1980. |
over Arabian Gulf. |
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Saudi Arabian Airlines, HZ-AHJ |
L-1011-200 (serial no 1161). |
An exploding tire blew a hole in the fuselage while in flight. Two
passengers were sucked out of the aircraft in the rapid decompression that
followed.
May 4, 1983. |
Miami-Nassau-Miami |
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Eastern Airlines, N334EA. |
L-1011-1 (serial no 1141). |
Flight 855 departed Miami for a 37 minutes trip to Nassau. When they
descended through 15000 ft the low oil pressure light for the #2 engine
illuminated. During the short flight all engines had indicated normal
pressure and quantity but now the #2 engine showed low level (~8 qts) and
pressure (~15-25 psi) while engines #1 and #3 still indicated normal. The #2
engine was shut down, the APU started, and with poor weather at Nassau the
Captain decided to return to Miami. The flight was now down at 12000 ft and
turned back towards Miami while climbing up to FL200.
When climbing through
15000 ft they got a low oil pressure light for the #3 engine. The Captain
retarded the #3 throttle slightly and reduced the rate of climb. Then the #1
engine low oil pressure light illuminated. The gauges at the Flight
Engineerīs panel showed that the oil pressure on both operating engines were
low and falling and that all quantity gauges indicated zero. Since the
risk of this happening is very slim the crew considered indication problems.
They levelled off at 16000 ft at 300 kt and told ATC about their problems.
ATC cleared them direct to Miami and speed was reduced to 230 kt.
Then, with no warning, the #3 engine failed. They were now flying on one
engine. They radioed Miami and was cleared for a straight-in approach for
runway 27L, still with 70 miles to go. They started a descend and also began
dumping fuel. The weather at Miami was good and the crew now realized that
the gauges were functioning properly. At 12000 ft also #1 engine failed.
They were now 55 miles from Miami with no engines at all running. The rate
of descend increased to 1600 ft/min with a speed of 225 kt and the crew now
tried to restart engine #2 through windmilling. It did not start.
The cabin was prepared for ditching. The Captain would set it down on the
water with the landing gear retracted, normal landing flaps and with the
nose pitched up at 12 degrees. That would probably torn off the wing
engines, flaps and horizontal stabiliser. The aircraft would still be
expected to stay afloat for 20-25 minutes.
There was little hope of any successful restart of the wing engines but
the crew tried it anyway, with no success. Now an airstarter assisted
restart of engine #2 was carried out and at 4000 ft, still with 22 miles
to Miami, it started. At 3000 ft they headed straight for runway 27L. On
landing both engines #1 and #3 smoked badly bacause the fuel switches
were still on from the previous start attempts and fuel was still beeing
pumped. Fire bottles were discharged on both those engines.
The Captain asked for a tug to tow the aircraft away from the runway but
was informed that there would be a delay for that. Then he tried to use the
#2 engine only to find that there was no power available. The #2 engine
failed on the runway.
The reason for all three engines losing all their oil was a magnetic chip
detector replacement, on all engines, the previous night. The installed chip
detectors were all missing their o-rings and when the engines were started
they began to leak oil. A ten-second engine motoring was carried out at
night to check for leaks but it was established later that a minimum of 30
seconds was required to get a leak with o-rings missing.
And about the start attempts on engine #2: The crew entered the chart
incorrectly and tried a windmill start when an airstarter assisted one
would be required. Later on, when they discovered that they needed
airstarter assist the engine started. If they would have entered the chart
correctly the first time - would the #2 engine have lasted all the way to
Miami?
Read the full story in Stanley Stewartīs book
"Emergency - Crisis on the Flight Deck".
August 02, 1985 |
Dallas, USA |
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Delta Airlines N726DA |
L-1011-1 (serial no 1163). |
DL191, from Fort Lauderdale, approached Dallas runway 17L in rain and
thunderstorm. A microburst forced the aircraft down 6300 ft short of the
runway. On impact it hit a car on a highway and struck two watertanks. It
caught fire and of the 163 people onbord 134 were killed.
May 3, 1986. |
Colombo, Sri Lanka. |
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Air Lanka 4R-ULD |
L-1011-100 (serial no 1061). |
The flight from Colombo, Sri Lanka to Male, Maldives was delayed. During
(the late) boarding a bomb, timed for an in-flight blast, exploded. Of the
128 people onboard, 14 were killed. The bomb, which destroyed the plane, was
hidden in the aircraftīs "Fly-Away-Kit".
This incident involved a rear pressure bulkhead failure due to fatigue.
The below AAIB report contain lotīs of technical details of L-1011
pressure bulkhead problems, including some info about this incident.
This incident involved a rear pressure bulkhead failure.
The below AAIB report contain lotīs of technical details of L-1011
pressure bulkhead problems, including some info about this incident.
Date unknown. |
Pacific Ocean. |
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Halfway between Los Angeles and Honolulu the Flight Engineer found the fuel
quantity in one of the tanks to be decreasing at an abnormal rate. The crew
decleared an emergency and started to crossfeed all engines from the leaking
tank, to save fuel in the other tanks until it was needed.
The aircraft was prepared for what looked like a ditching and the
Honolulu Coast Guard had been alerted for a possible intercept and resque
operation. However, this was a lucky day, and they landed with very little
fuel left onboard. The reason for the leak was a faulty fuel line.
June 28, 1991. |
Dusseldorf, Germany. |
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LTU, D-AERI. |
L-1011-1 (serial no 1114). |
Aircraft destroyed by fire while undergoing maintenance (welding) in hangar.
The ground crew managed to tow the aircraft out of the hangar, limiting the
damages to only this aircraft.
July 30, 1992. |
New York JFK, USA. |
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Trans World Airlines (TWA) N11002. |
L-1011-1 (serial no 1014). |
The aircraft took off from runway 13R at New Yorkīs JFK airport with 292
people onboard. When it became airborne, with the First Officer at the
controls, the stickshaker was activated. The Captain took control of the
aircraft and aborted the takeoff. Touchdown was made at 14 ft/sec (design
limit 6 ft/sec) after 6 seconds in the air. Maximum brake and reverse was
used and when the Captain understood that they could not stop before the
runway end, he turned it to the left onto the grass. The airplane caught
fire and was destroyed. The right Angle of Attack sensor had experienced 9
previous malfunctions, not detectable during cockpit preflight tests. The
sensor gave a false warning when the airplane became airborne.
June 20, 1995. |
Between Tenerife South and Faro. |
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Caledonian Airways, G-BBAH. |
L-1011-100 (serial no 1101). |
The aircraft departed Tenerife South for a flight to Manchester with 401
passengers onboard. I hour into the flight, at FL310, there was a loud
"muffled bang" and a feeling of pressure in the ears. The Flight Engineers
instrumentīs revealed that the cabin altimeter was climbing at approximately
2000 ft/min. The cockpit crew donned their oxygen masks and commenced an
emergency descend. The Captain was now flying manually and the First Officer
handled the radios. They were in contact with Casablanca Radio and radioed
their emergency on that frequency.
In the cabin the crew also heard the bang (except for one attendant in
lower galley) and felt pressure in their ears. The purser went to the Flight
Engineer and told him that the oxygen masks were not deployed in the cabin.
The F/E did that manually. The automatic system had not yet been activated
because the cabin had not reached the preset altitude at that time. There
was a smell of burning in the cabin because of the heat the oxygen
generators produced.
The Captain levelled off at FL100 after a descent at a speed slightly
less than the maximum operating speed. All system were found to be normal
after the descend except for a "truck" light on the gear. The descend had
been done with gear down.
At this time, the First Officer had established contact with Lisbon ATC.
The aircraft position was approximately halfway between Tenerife and Faro
so the Captain decided to divert to Faro. During the flight to Faro 4000 kg
of fuel was dumped to bring the landing weight down to 160 000 kg.
The cabin was prepared for an emergency landing because of the landing
gear "truck" light. As speed was reduced on final the "truck" light went
out and the landing was normal.
The decompression was caused by a partial rupture (~300 x 400 mm) of the
rear pressure bulkhead. The below AAIB report contain lotīs of technical
details of this and other L-1011 pressure bulkhead problems.
August 23, 1995. |
Pacific Ocean. |
|---|
Delta Airlines N781DL. |
L-1011-1 (serial no 1003). |
The aircraft was cruising at FL330 when a sudden decompression occured. The
flight, with 236 people onboard, was at this time 450 miles west of the
departure airport, Los Angeles. Destination was Honolulu. It landed safely
even though the airframe was severly damaged. The aircraft is now used for
ground tests by Lockheed.
October 31, 1996. |
Gatwick, London, England. |
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Caledonian Airways, G-BBAH. |
L-1011-100 (serial no 1101). |
Engine #2 was started during pushback. After that, engine #3 was started but
it failed to rotate so the start was abandoned. Engine #1 was then started
with the intention to make another try at #3 after that. When #1 was started
ATC reported smoke and flames from the tail of the aircraft. The crew had
not observed that #2 TGT had increased and reached 250 degrees after 3
minutes.
The Airport Fire Service reacted very rapidly and sprayed the engine with
foam. The crew were initially unaware of this action. Engineering assessed
that the engine had suffered thermal shock from the foam and that corrosion
damage had possibly occured to the adjacent aircraft structure. The fuel
flow regulator was believed to be faulty.
March 27. 1997. |
New York, USA. |
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Delta Airlines N762DA. |
L-1011-500 (serial no 1210). |
The L-1011 was pushed back from the gate by a groundcrew of 3 employees.
The tug operator was seated facing the airplane, while wing walkers were
placed at the left and right wing tips. When the forward motion was
initiated, the left and right wing walkers started to converge towards the
tow bar, anticipating the disconnect of the airplane when it stopped. The
left wing walker observed the right wing walker, the designated Dispatch
Agent (DA) for the flight, approach the tow bar. The left wing walker
glanced at the left wing tip, and when his vision returned to the tow bar,
he saw the right wing walker under the nose wheel of the airplane. He was
fatally injured.
May 15, 1997. |
Saint Louis, USA. |
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Trans World Airlines (TWA) N11003. |
L-1011-1 (serial no 1015). |
During climb passing FL290 the crew heard a loud bang. No abnormalities were
found except for some vibrations near the left wing area. After landing at
destination it was found that the left gear strut door had separated from
the aircraft. Other damages from that failure was also detected.
August 7, 1997. |
Honolulu, Hawaii, USA. |
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Delta Airlines, N740DA. |
L-1011-250 (serial no 1244). |
After maintenance completed troubleshooting and the aircraft taxied out for
the final time, the aircraft had taxied 11.3 miles within a 3-hour period.
There was no temperature gauge or tabular data available that could have
informed the crew that heat buildup resulting from taxi distance was now at
a level that potentially threatened the integrity of the tires.
During the takeoff roll, the 3F tire exploded, resulting in vibration,
shudder, and yaw. The sudden instability, combined with a phantom C1 cargo
door light, caused the Captain to abort. The abort was initiated about Vr
(165 knots) with approximately 6,000 feet of runway remaining. As the
aircraft came to a stop, the nose wheels were 164 feet short of the overrun
area for runway 8R. A brake fire began while the aircraft was stopping and
the captain directed an emergency evacuation.
The 2R and 4R doors failed to open, and the 4L and 3L doors were not used
due to their proximity to the fire and smoke. The 4R door was jammed by a
broken piece of backboard, and the 2R door malfunctioned due to a partially
broken counterbalance spring. The flight attendant who attempted to open the
2R door did not attempt to manually lift the door. All evacuations were made
through the 1L, 1R, 2L, and 3R doors.
Firefighters had difficulty communicating with the flight crew and in
verifying the total number onboard because the airline's passenger count
does not include lap children. A total of 56 passengers and 2 flight
attendants were treated for minor injuries, while 1 passenger received a
broken ankle. All injuries were attributed to the use of the slides.
Passengers failed to follow flight attendants and attempted to evacuate with
their carryons. The airline did not effectively supervise the passengers
after the evacuation and several began walking toward an active runway.
An inspection of the 3R tire showed bead separation had occurred. The
estimated bead temperatures during the takeoff roll reached between 350 and
400 degrees Fahrenheit. The bead begins to degrade between 250 and 280
degrees Fahrenheit.
October 20, 1997. |
Gatwick, London, England. |
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Air Transat, C-FTNG. |
L-1011-150 (serial no 1048). |
When the aircraft started to accelerate at Gatwick runway 08R, "Hydraulic
System" and "Flight Control Panels" warning lights illuminated on the
"Warning and Caution Panel" (CAWP). "Rudder Hydraulic Limiter Push"
illuminated on the overhead panel as well as "J Area Overheat" and hydraulic system
A "Low Pressure Output" on the Flight Engineerīs panel. Hydraulic system A
quantity gauge also indicated loss of fluid. The Captain aborted the takeoff
and at the same time the tower radioed that smoke was coming from one of the
engines.
The aircraft slowed down on the runway, max speed had only been 68 kt,
and taxied off and stopped on a high-speed exit. Fire and resque crew saw
that smoke was coming from the leading edge of the tailplane and from a
grill at the bottom of the fuselage. Cabin crew also reported light smoke
entering the cabin in the rear.
A controlled evacuation was initiated using the two front slides on each
side of the aircraft. It took 10 minutes to evacuate 357 passengers and 11
suffered minor injuries.
Examination showed that an elbow section of a large bore titanium duct,
delivering air from No 2 engine bleed system, had blown out. This had caused
secondary damage to adjacent hydraulic pipes in 'A' and 'B' systems which
accounted for the observed hydraulic system failures. Further examination
showed that the failure had been caused by a massive over pressurisation of
the air duct.
February 06, 1998. |
Panama City, Panama. |
|---|
American Int`l Airways, N103CK. |
L-1011-200F (serial no 1212). |
---This is preliminary information, subject to change, and may contain errors.---
American International Airways (Connie Kalitta Services) flight 840,
experienced blown tires during an aborted takeoff from the Tocumen
International Airport, Panama City, Panama. Visual meteorological conditions
prevailed at the time and an IFR flight plan was filed for the nonscheduled,
international, cargo flight. The airplane was not damaged and the airline
transport-rated captain, first officer, flight engineer, and two additional
crewmembers were not injured.
The flight was originating at the time of the incident. According to
officials from the Government of Panama, the captain elected to use a runway
that was 2,000 feet shorter than the longer of the parallel runways. During
the takeoff after the nose landing gear was rotated the captain elected to
abort. After touchdown all main landing gear tires were blown and the
airplane was stopped on the runway.
May 31, 1998. |
Manchester, England. |
|---|
EI-COL. |
L-1011-1 (serial no 1036). |
The aircraft was flown manually for a landing at Manchester runway 24R.
Landing data card showed a landing weight at 304 000 lb with a VREF at 129
kt. The pilot handling the aircraft felt that the rate of descend did not
reduce as normal during the flare so he increased the pitch attitude which
resulted in a tail strike. After touchdown the Flight Engineer commented
that the pitch attitude at touchdown was about 15 degrees. Only minor damage
occured to a drain mast, antenna, tail bumper and a small skin area.
The DFDR was malfunctioning and contained no data. A final approach
profile could still be constructed using height calls from the CVR and
recorded radar data. That profile showed that the rate of descend increased
below 100 ft AGL and that the flare appeared to be ineffective.
Company procedures was that the Captain prepared the loadsheet, in lbs,
and the Flight Engineer calculated Take Off and Landing Data Cards. At the
departure station all figures were given in kilos. They were converted to
lbs except for passenger weight which was still in the kilo figure on the
loadsheet. This meant that the aircraft was 22 000 lbs heavier than the
loadsheet figure. The correct VREF for the landing should have been 136 kt.
On the previous sector the loadsheet contained exactly the same mistake
but that approach was flown by the other pilot at a slightly higher speed
with a normal landing.
December 22, 1998. |
Atlanta, Georgia. |
|---|
Delta Airlines, N766DA |
L-1011-500 (serial no 1207). |
---This is preliminary information, subject to change, and may contain errors.---
Just before pushback from the gate, a passenger seated immediately aft
of L2 door, saw sparks and smoke from a vent below the sidewall panel. The
Captain was notified and everyone left the aircraft through the forward
exit. The flight was cancelled.
Maintenace personnel was called for and down in the MESC, they found two
wire bundles, about 3 inches in diameter, that were burnt. The wire bundles
were coloured blue from leaking toilet fluid. The wire bundles were repaired
and the aircraft was back in service after 6 days.
The mid toilets on Delta aircraft have a "low charge level" and therefor
have an increased risk of beeing overfilled. In that case the excessive
fluid may end up on electrical wiring.
Delta Airlines now has a "Special Inspection" of the wires, the toilet
drip pan and the drain tubes in the MESC. There has been a great number of
reports of fluid, dirt, dust and metal debris in the inspection area.
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rapid decompression over Arabian Gulf in 1980.
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